Huck's new daily - Victory Red '05 CCSSB

So after some math, I made some shim adjustments. First try, I moved the carrier over to the pass side .010 and I believe I moved the pinion away from the carrier .005.

.004, too tight. Phooey

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More math and playing with shim packs

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Finally got it in spec, .007. Spec is .006-.010

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Run another pattern, not bad, I think we're gonna try it

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Time to put the final pinion bearing on

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Borrowed a coworker's split beam torque wrench to properly check drag on the pinion. Still odd has marks but much better than my 0-800in lbs one. Didn't get any pictures but I took a big chance and did the crush sleeve with an impact. Spec on the drag is 14-19in lbs and you add a couple for the pinion seal. I nailed it right at 20in lbs. Score

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So then I go to pull out the cross pin so I can install the axles...can't get it out. I'd read about this years ago but forgotten that for most gearsets 4.88-up, you have to grind down a tooth to clear the pin. Didn't feel like doing that this day so I moved onto the front axle. Needed a change of pace.

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Did I mention this thing lived on dirt roads and had an oil leak? lol

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First thing was getting the sway bar and center link/TRE's out of the way

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Pulled the bolts out of the CVs and drained the fluid

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We're gonna pretend we didn't see all that...

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Fixed

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Couldn't even see the rear mount for all the caked on crud

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4 bolts, some sketchy-ness on the trans jack and we're down

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This is my first time dropping a front diff and other than getting the center link free of the idler/pitman arms, it's super easy. I'll never attempt an oil pan reseal in a 4wd without pulling the diff down

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The engine leaks from every orifice just about

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Started disassembly by removing the pass side/long side extension housing

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The stub shaft and thrust washer stayed in

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Pulled those out to expose the side adjuster

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This is looking at the pass side extension housing, this is what the front axle actuator does. Just slides a shift fork and gear over the stub shaft to engage everything

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Pulled the other stub shaft out with a pry bar

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And pulled the vent out

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The inside looked pretty clean, the gear, the carrier and the spiders all looked good

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Carefully split the case, gotta go slow cuz it's aluminum

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The bearings are a little chewed up and dark, I think they got hot

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There's a light blue hue to the races too, these things got hot. I'm assuming he probably forgot it was in 4wd (probably more than once) and ran it like that for a while. Or low on fluid, or both. Even though the fluid I drained out looked good, it'd probably been changed

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The pinion bearing races look bad too

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So then I take a few measurements of the side adjusters to have a starting point.

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I was actually able to just knock them out without turning them so I just left them alone for reassembly

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And the other side. This one, the race fell out on it's own before I tapped out the adjuster

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I'm tell ya, if you think you'll ever do axle work, buy this bearing puller. It is an absolute godsend. Although I was informed after this that I should be using the race to help further support the bearing. Not a big deal for bearings you're not gonna reuse but definitely important if you are

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And this is what an exploded 8.25 looks like

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So then reassembly started a few days later. New pinion races pressed in

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Forgot to take pictures but I had to pull the cir clip off this axle with a pick to get it to come out so I could replace it's axle seal

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Snuck the ring gear up carefully with the bolts

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Threw the pinion in with the setup bearings (same ones from the rear end) and no crush sleeve or seal, adjusters back in, new races and ready to put the halves back together for a test fit

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Remember, I'd left the adjusters in the factory positions. That wouldn't even allow the case halves to sit down together. I played with it a few times and finally just said fuck it and ran the driver's side one all the way out. Finally the case halves would seat

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Then I started sneaking up on the passenger side adjuster till it had some tension. Unfortunately that special spanner tool I had is the wrong one, it's wayyy too big to even fit down in this section of the case and the pins are too far apart, they wouldn't even work in the adjusters anyway

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So once it seemed to spin pretty well, I rigged it up to measure backlash

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Big ole honkin' Dodge Durango battery works great for holding the case still

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So spec here is the same as the rear, .006-.010. Since you're measuring at the yoke and not on the ring gear, you have to divide by 2. This is extremely hard to do and it takes a while to get the "feel" to know you're in the right range. And each reading came out a point or two different, so I was just shooting for a good range. I fiddled with this for probably an hour before I felt comfortable with my results. Ended up getting .016-.019 consistently, which puts me at .008-.0095, perfect. Time to paint.

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Not a bad pattern. I'm still playing with my paint+gear oil mixture but this isn't bad. And for a front diff that only occasionally gets used, I decided to call that good and run it.

Coast side

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Drive side

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There were several maths involved in getting here

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I heated the final assembly bearing up in the toaster oven at 250* for ~30min while the pinion was in the freezer and I ate dinner. Plopped right on.

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So then it was time to put the pinion in with the crush sleeve and pinion seal. This SUCKED ASS. I didn't wanna risk this one with the impact so I used my coworker's pinion holder and a breaker bar. I started with my 1/2" breaker and it didn't take long before it started to spread the ears on that one. I got frustrated and grabbed the impact, thankfully I remembered that the boss has a 3/4" set so I grabbed that breaker bar and a jack handle. That worked really well.

But I was sneaking up like 1/4" of rotation at a time for nearly 1.5hrs before I finally got the drag in spec. These are a little different than the rear axle, the rear axle you can tighten the nut down until you have the front to back "slop" out of the pinion and then worry about crushing the sleeve. But the front axle, you start getting into the crush sleeve long before you're out of "slop" in the pinion. Not fun.

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When I got done I just laid on the floor for a few minutes, that was a MF'r lol

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Then back on the bench to double check that I'd see the drag correctly, it was hard to judge on the floor. I did thankfully

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Back on the bench one more time to check backlash and pinion drag, both stayed in spec

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Axle seals, extension housing and both stub shafts back in

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Vent in, ready to go back in the truck

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So back to the rear, I pulled the carrier back out to do my grinding on that one tooth to let the cross pin come out

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Then axles in. It was no picnic getting the C-clips back in, they're gonna SUCKKK to get back out if I ever have to

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Done, cover on and torqued, full of fluid

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So then we move onto the driveshaft. A balljoint press makes quick work out of this

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Crazy how much is still original on this truck. They last a long time if you don't screw with them like we do lol

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First U-joint from the parts store was a fail, the zerk wouldn't fit without hitting either the driveshaft or the yoke on the rear end

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That's better

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All in with new clips and good to go

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Also tried to buy new straps/hardware cuz I had 1 bolt head start to round off on me. WTF is this shit!? So I was just careful with everything going back in.

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So once all that was done and I ate lunch and ran a couple errands to let the gasket maker setup up, I decided to run it on the lift. It all sounded ok like that but I wasn't running it fast and wasn't about to get out with the wheels turning since I was by myself. But 2wd and 4wd both sounded fine, so down and on the ground for a test drive.

Got ~50yds out the door and start hearing a faint rotational sound. Almost like I can hear the teeth meshing in the rear end. Doesn't sound bad, just a sound. Almost sounds like I have too much backlash or the pinion moved on me.

So then I go around our building into the dirt on the backside to test 4wd and make sure it doesn't bind up. Seems good in 4lo. So put it back in 2wd and get back on the pavement for a long straight run. Put it in 4hi and over 10-15mph I have a terrible bearing roar. Dammit.

So both axles need to come back apart. Phuck my life.